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dc.contributor.authorOwen, Philip Rayen_US
dc.contributor.otherMassachusetts Institute of Technology. Gas Turbine Laboratoryen_US
dc.date.accessioned2016-10-06T21:22:24Z
dc.date.available2016-10-06T21:22:24Z
dc.date.issued1986en_US
dc.identifier.urihttp://hdl.handle.net/1721.1/104749
dc.descriptionOctober 1986en_US
dc.descriptionAlso issued as: Thesis (M.S.)--Massachusetts Institute of Technology, Dept. of Aeronautics and Astronautics, 1986en_US
dc.descriptionIncludes bibliographical references (pages 57-58)en_US
dc.description.abstractThe unsteady flow about a section of a modern first stage transonic compressor rotor was simulated using a finite difference approximation to the two-dimensional, Reynolds averaged, unsteady, compressible, viscous Navier-Stokes equations. The computation was performed in both steady state and time-accurate modes, and the results compared. The time-accurate results were analyzed in some detail. Two frequency regimes were observed. High frequency unsteadiness due to vortex shedding was found at frequencies varying between 11 KHz and 19 KHz. A low frequency cycle was also observed at 365 Hz. The low frequency cycle produced significant variations in blade force and moment. It also modulated the strength and frequency of the vortex shedding. Arguments were advanced to explain the mechanics of the vortex street formation in terms of a single free shear layer instability. The variations in shedding strength and frequency were related to movement of the separation point. A wholly satisfactory normalization of the frequencies was not found. The low frequency cycle was analyzed as a quasi-steady sequence of events stemming from movement of a shock wave spanning the blade passage. The possibility was entertained that the cycle was due to purely numerical sources, but no likely mechanism was found.en_US
dc.description.sponsorshipSponsored by Allison Gas Turbine Division of General Motorsen_US
dc.description.sponsorshipSponsored by the Air Force Office of Scientific Research, Multi-investigator contract. F49620-86-C-0018en_US
dc.format.extentviii, 122 pagesen_US
dc.publisherCambridge, Mass. : Gas Turbine Laboratory, Massachusetts Institute of Technology, [1986]en_US
dc.relation.ispartofseriesGTL report #189en_US
dc.subject.lccTJ778.M41 G24 no.189en_US
dc.subject.lcshImpellersen_US
dc.subject.lcshRotorsen_US
dc.subject.lcshFluid dynamicsen_US
dc.titleComputational simulation of unsteady flow in transonic compressor rotoren_US
dc.typeTechnical Reporten_US
dc.identifier.oclc26943794en_US


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