Show simple item record

dc.contributor.advisorAlan H. Epstein.en_US
dc.contributor.authorParker, David V. (David Vickery)en_US
dc.contributor.otherMassachusetts Institute of Technology. Dept. of Aeronautics and Astronautics.en_US
dc.date.accessioned2006-03-29T18:44:11Z
dc.date.available2006-03-29T18:44:11Z
dc.date.copyright2005en_US
dc.date.issued2005en_US
dc.identifier.urihttp://hdl.handle.net/1721.1/32433
dc.descriptionThesis (S.M.)--Massachusetts Institute of Technology, Dept. of Aeronautics and Astronautics, 2005.en_US
dc.descriptionIncludes bibliographical references (p. 111-112).en_US
dc.description.abstractA unique counter-rotating aspirated compressor was tested in a blowdown facility at the Gas Turbine Laboratory at MIT. The facility expanded on experience from previous blowdown turbine and blowdown compressor experiments. Advances in thermocouple and facility designs enabled efficiency estimates through total temperature and total pressure measurements. The facility was designed to provide at least 100 ms of available test time, approximately a factor of five greater than previous blowdown compressor facilities. The adiabatic core efficiency of the compressor was estimated with an uncertainty of 0.8% and the corrected flow was estimated with an uncertainty of 1.0%. The compressor was tested at several operating conditions and two speed lines were partially mapped. The maximum measured total pressure ratio across the two stages was 3.02 to 1. The measured adiabatic efficiency for that point was 0.885. The span-wise total pressure, total temperature, and efficiency profiles were compared to the predicted profiles for runs with the corrected speeds of the two rotors at 90% of design and 100% design. There appears to be reasonable agreement between the predictions and the measurements.en_US
dc.description.statementofresponsibilityby David V. Parker.en_US
dc.format.extent141 p.en_US
dc.format.extent7485237 bytes
dc.format.extent7492657 bytes
dc.format.mimetypeapplication/pdf
dc.format.mimetypeapplication/pdf
dc.language.isoengen_US
dc.publisherMassachusetts Institute of Technologyen_US
dc.rightsM.I.T. theses are protected by copyright. They may be viewed from this source for any purpose, but reproduction or distribution in any format is prohibited without written permission. See provided URL for inquiries about permission.en_US
dc.rights.urihttp://dspace.mit.edu/handle/1721.1/7582
dc.subjectAeronautics and Astronautics.en_US
dc.titleDesign and operation of a counter-rotating aspirated compressor blowdown test facilityen_US
dc.title.alternativeCounter-rotating aspirated compressor blowdown test facilityen_US
dc.typeThesisen_US
dc.description.degreeS.M.en_US
dc.contributor.departmentMassachusetts Institute of Technology. Department of Aeronautics and Astronautics
dc.identifier.oclc61718567en_US


Files in this item

Thumbnail

This item appears in the following Collection(s)

Show simple item record