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dc.contributor.advisorDavid L. Carter and Harry L. Tuller.en_US
dc.contributor.authorSakai, Marken_US
dc.contributor.otherMassachusetts Institute of Technology. Dept. of Materials Science and Engineering.en_US
dc.date.accessioned2006-07-13T15:21:13Z
dc.date.available2006-07-13T15:21:13Z
dc.date.copyright2005en_US
dc.date.issued2005en_US
dc.identifier.urihttp://hdl.handle.net/1721.1/33401
dc.descriptionThesis (S.M.)--Massachusetts Institute of Technology, Dept. of Materials Science and Engineering, 2005.en_US
dc.descriptionIncludes bibliographical references (p. 103-106).en_US
dc.description.abstractThis thesis presents fabrication process improvements for a RF MEMS resonator for the purpose of improving the quality factor (Q) and extending the frequency range. The process changes include the use of conformable contact lithography (CCL) and chlorine-based dry etching for improved fine-feature patterning and Moiré -based alignment techniques to allow for a non-self-aligned process. The resulting control over feature size and structure are expected to improve Q and enable higher frequency resonators. A CCL process utilizing moir6 alignment marks is described. An automated Moiré -based alignment system using Labview software is presented which demonstrates sub-100 nm alignment accuracy for a single alignment mark. A full-wafer alignment experiment is described that demonstrates average pattern placement errors of ... for the x- and y-directions respectively. The experimental limitations are analyzed and suggested improvements to the system are detailed. Chlorine dry etching experiments are conducted in order to produce a straight sidewall etch through the "stack" of resonator materials (chrome, aluminum nitride, and molybdenum). A combination of Cl₂/0₂, Cl₂/Ar, and CF₄0₂ plasmas at low pressure (2 mTorr), high microwave/source power (500W), and a moderate DC bias (-150V) demonstrates a straight sidewall angle (>80⁰ measured from horizontal) with no undercut for all layers of the stack. RF resonators fabricated with these process modifications are presented. An average overlay error of 55 nm (110 nm min-max) is recorded for 11 devices located closest to the line between the alignment marks in an aligned release of the resonators. The design modifications enabled by the new process are described and the prospect for higher-frequency devices and higher-Q device performance is discussed.en_US
dc.description.statementofresponsibilityby Mark Sakai.en_US
dc.format.extent106 p.en_US
dc.format.extent5996459 bytes
dc.format.extent6000901 bytes
dc.format.mimetypeapplication/pdf
dc.format.mimetypeapplication/pdf
dc.language.isoengen_US
dc.publisherMassachusetts Institute of Technologyen_US
dc.rightsM.I.T. theses are protected by copyright. They may be viewed from this source for any purpose, but reproduction or distribution in any format is prohibited without written permission. See provided URL for inquiries about permission.en_US
dc.rights.urihttp://dspace.mit.edu/handle/1721.1/7582
dc.subjectMaterials Science and Engineering.en_US
dc.titleFabrication process changes for performance improvement of an RF MEMS resonator : conformable contact lithography, Moiré alignment, and chlorine dry etchingen_US
dc.typeThesisen_US
dc.description.degreeS.M.en_US
dc.contributor.departmentMassachusetts Institute of Technology. Department of Materials Science and Engineering
dc.identifier.oclc62708851en_US


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