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dc.contributor.advisorStanley Gershwin and Larry Wein.en_US
dc.contributor.authorZhou, Ning, 1970-en_US
dc.contributor.otherMassachusetts Institute of Technology. Dept. of Mechanical Engineering.en_US
dc.date.accessioned2005-08-22T23:34:29Z
dc.date.available2005-08-22T23:34:29Z
dc.date.copyright2000en_US
dc.date.issued2000en_US
dc.identifier.urihttp://hdl.handle.net/1721.1/9214
dc.descriptionThesis (M.B.A.)--Massachusetts Institute of Technology, Sloan School of Management; and, (S.M.)--Massachusetts Institute of Technology, Dept. of Mechanical Engineering, 2000.en_US
dc.descriptionAlso available online at the DSpace at MIT website.en_US
dc.descriptionIncludes bibliographical references (leaf 77).en_US
dc.description.abstractFab 17 was a Digital Equipment Corporation semiconductor manufacturing and development facility. In June of 1998, Intel purchased Fab 17 from Digital. Intel shifted the focus to manufacturing and implemented many Intel operation policies. Intel sold equipment back to Digital and reorganized the manufacturing organization. As a result of Intel's initiatives and increasing demand for Fahl 7 products, Fab 17's profitability was improved. Despite improved profitability, Fab 17 was not meeting line yield performance goals. This thesis examines line yield excursions at Fab 17. Root causes are identified, and recommendations are made. The thesis first analyzes the line-yield loss data at Fahl 7 from a macro perspective. Inexperienced technicians and multitasking are found to be associated with most line yield incidents. The thesis then studies line yield excursions in high leverage functional areas in detail. Two major root causes are identified. First, in the reorganization, many technicians switched to new roles and had to be retrained. The training was rushed. Due to low level of automation, processing wafer at Fab 17 requires experience and proficiency. Fab 17's wafer starts increased in the first two quarters of 1999. Technicians had to rush to process the wafers. This resulted in high stress, which leads to high probability of line yield excursion. The inexperienced technicians are even more prone to line yield excursions under high stress. In addition, Fab 17 lacked a minimum staffing policy. Often an inappropriate number of technicians are present on the manufacturing floor. This necessitates multitasking, which creates higher stress and leads to higher probability of line yield excursions. The thesis recommends operations policies to address these issues and reports the actual implementation and some preliminary results.en_US
dc.description.statementofresponsibilityby Ning Zhou.en_US
dc.format.extent77 leavesen_US
dc.format.extent5251889 bytes
dc.format.extent5251650 bytes
dc.format.mimetypeapplication/pdf
dc.format.mimetypeapplication/pdf
dc.language.isoengen_US
dc.publisherMassachusetts Institute of Technologyen_US
dc.rightsM.I.T. theses are protected by copyright. They may be viewed from this source for any purpose, but reproduction or distribution in any format is prohibited without written permission. See provided URL for inquiries about permission.en_US
dc.rights.urihttp://dspace.mit.edu/handle/1721.1/7582
dc.subjectSloan School of Management.en_US
dc.subjectMechanical Engineering.en_US
dc.titleImproving line yield at Fab17en_US
dc.typeThesisen_US
dc.description.degreeS.M.en_US
dc.description.degreeM.B.A.en_US
dc.contributor.departmentMassachusetts Institute of Technology. Department of Mechanical Engineering
dc.contributor.departmentSloan School of Management
dc.identifier.oclc45489686en_US


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